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Tag: National Transportation Safety Board

  • Political and aviation leaders look at safety issues at DCA and possible improvements – WTOP News

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    In the aftermath of the Jan. 29, fatal midair collision near Reagan National Airport, two Virginia congressional leaders discussed on Friday the ways to make the airport and the entire national aviation network safer.

    In the aftermath of the Jan. 29 fatal midair collision near Reagan National Airport, two Virginia congressional leaders discussed on Friday the ways to make the airport and the entire national aviation network safer.

    But Virginia Sen. Mark Warner and Rep. Don Beyer, who represents the state’s 8th District, acknowledged during a roundtable discussion in Alexandria that it will require leadership from government officials and some new regulations about operations around the highly congested airspace around Reagan National.

    Many federal agencies have agreed that the airspace around Reagan is among the most complicated and congested in the country. Beyer said part of the challenge is that Reagan is operating at 40% above its designed capacity.

    “Every time we board a plane, we have to trust that we built a system that is going to get us there,” he said. “The airport was designed for 14 million passengers, and it is doing 25 million per year, and the busiest runway in the United States.”

    Beyer said he is frustrated that the Army is blocking his request to open an investigation into the Jan. 29 crash, despite a bipartisan request by at least two dozen senators.

    He plans to submit legislation to force the Army to do that, and Senate Commerce Committee Chairman Ted Cruz, R-Texas, has also proposed a similar bill to look into what Cruz calls “systemic breakdowns” that could have been a factor in the nation’s deadliest aviation crash in more than 20 years.

    Sixty-four passengers and crew members on an American Airlines regional jet and three crew members in an Army Black Hawk helicopter died when the Black Hawk hit the jet as the passenger plane was on its final approach to Reagan National. Both aircraft plunged into the icy waters of the Potomac River.

    Both Warner and Beyer have been longtime opponents of adding flights at Reagan and they fought a measure in the last Congress to add five more long-distance flights from the airport to the West Coast. Ultimately, that measure passed Congress in the new Federal Aviation Administration Reauthorization Bill and was signed into law by President Donald Trump.

    Beyer and Warner are calling for an independent review of the entire region’s airspace, with the possibility that the number of flights might have to be reduced at Reagan.

    One of those speaking at the session was Matthew Collins, who lost his younger brother Chris in the crash.

    “How do we honor these 67 people and prevent something like this from ever happening again?” Collins said.

    Former pilots, air traffic controllers and other aviation stakeholders also presented recommendations and ideas to Warner and Beyer, and the two said they will discuss many of them with the Federal Aviation Administration and others to improve safety.

    Beyer and Warner said the Army has voluntarily cut the number of helicopter flights from the Pentagon’s nearby helipad and helicopter specific routes have been closed and moved further south from Reagan. But now, some residents in those flight paths are complaining about aircraft noise from the helicopters.

    In May, after another close call involving military aircraft and two planes that were landing at Reagan National, forcing both to abort their landings, the FAA put new restrictions on Army helicopter flights from the Pentagon.

    In August, the Department of Transportation’s Office of Inspector General started an audit of the FAA’s airspace management and the FAA’s allowance of exemptions of what is called ADS-B, or Automatic Dependent Surveillance-Broadcast. That’s a GPS-based monitoring system in aircraft that gives pilots significantly more information about where other aircraft are, in relation to where their aircraft is located.

    Because of the information it provides, ADS-B is considered an upgrade over the existing radar technology.

    On the night of the Jan. 29 crash, the Black Hawk helicopter had an ADS-B system onboard, but it was turned off.

    On a national level, Warner said he is still very concerned that even as the FAA says it is rapidly training more air traffic controllers, the system is still short an estimated 3,000 controllers to bring it up to the full complement of controllers.

    “How are we going to get the personnel in terms of FAA air traffic controllers and others whose really job is the front line of keeping us safe?” he asked.

    The National Transportation Safety Board investigation is ongoing and a final report from the safety agency is expected sometime in the first or second quarter of 2026.

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    Dan Ronan

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  • Plane crash near Cambridge Airport leaves pilot dead

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    Parents of Annunciation shooting victims call for action, and more headlines



    Parents of Annunciation shooting victims call for action, and more headlines

    04:28

    Federal authorities say they’re investigating what has now been confirmed as a fatal plane crash in Cambridge, Minnesota.

    A social media post from the National Transportation Safety Board says the crash involved a Beech K35 airplane. 

    The Isanti County Sheriff’s Office says the plane crashed near the Cambridge Municipal Airport, located on 329th Avenue Northwest. When emergency crews arrived around 11:30 a.m. Thursday, they found the pilot, identified as a male, dead at the scene, according to a release from the city of Cambridge. 

    Both the NTSB and the Federal Aviation Administration will be investigating the incident. The FAA’s preliminary report said the plane “crashed under unknown circumstances.”

    Cambridge is about 55 miles north of Minneapolis. 

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    Krystal Frasier

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  • Pilot injured after airplane crashes, catches fire in Livingston County

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    A pilot suffered “significant injuries” after an aircraft crashed and caught fire Aug. 28 in a field in Unadilla Township, according to the municipality’s police department.

    The small, single-engine aircraft crashed and caught fire around 3:51 p.m. at the southern end of Richmond Field, the Unadilla Township Police Department wrote on Facebook. The township is located between Stockbridge and Pinckney.

    Livingston County Central Dispatch received a crash detection notification from an iPhone, followed by calls from nearby residents. First responders found the pilot outside the aircraft, according to police.

    The pilot, a 22-year-old man from Ohio, was flying from Charlevoix to Toledo, according to police. He was taken by ambulance to the University of Michigan Hospital.

    Stay informed and connected: Download our app to receive the latest updates on important news

    The cause of the crash is unknown. Unadilla Township police, the Federal Aviation Administration and the National Transportation Safety Board are investigating.

    Anyone who may have witnessed or heard the crash is asked to call 734-498-2325.

    — Contact reporter Evan Sasiela at esasiela@livingstondaily.com. Follow him on X @SalsaEvan.

    This article originally appeared on Livingston Daily: Pilot injured after airplane crashes, catches fire in Livingston County

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  • Close call with passenger jet happened after Army helicopter tried to land without clearance, preliminary report confirms – WTOP News

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    A Pentagon-bound Army helicopter that got less than half a mile from a commercial flight landing at nearby Ronald Reagan Washington National Airport in May did not have the proper clearance from Pentagon air traffic controllers, a preliminary report from the National Transportation Safety Board said Friday.

    The air traffic control tower at Reagan National Airport in Arlington, Virginia.

    Washington (CNN) — A Pentagon-bound Army helicopter that got less than half a mile from a commercial flight landing at nearby Ronald Reagan Washington National Airport in May did not have the proper clearance from Pentagon air traffic controllers, a preliminary report from the National Transportation Safety Board said Friday.

    At their closest, the Black Hawk helicopter and landing Delta Air Lines regional jet were only four tenths of a mile apart and separated by just 200 feet of altitude, causing controllers in the airport tower to force the jet to abort its landing.

    The helicopter was approaching the Pentagon from the southwest as three planes were preparing to land at Reagan National Airport, including an American Airlines regional jet arriving from Maine, a Delta flight from Orlando and the Delta regional jet from Boston involved in the close call.

    The report said the Black Hawk pilots coordinated their landing plans with the air traffic control tower at Reagan National Airport — which made for space for the helicopter between the American and later Delta flight — but controllers from a different air traffic control facility slotted the other Delta plane into that gap.

    When the helicopter pilot reported they were confident they could land, the airport controller told the Delta flight from Orlando to go-around and circle the airport.

    The NTSB report notes the helicopter pilot then attempted to land at the Pentagon helipad without getting clearance from the controller there, and when questioned aborted the landing and circled for another attempt.

    “When the (heliport) controller queried the crew to ask who had cleared them to land, the crew advised they were executing a go-around,” the report says.

    “Simultaneously,” to the helicopter again confirming to the airport tower it was landing, the controller there saw the Black Hawk “climb back up above the Pentagon building and immediately issued a go-around” to the approaching regional jet, according to a post-incident interview, the NTSB said.

    The NTSB also noted some of the controllers in the airport control tower were working two positions at the time of the close call. The local controller, who was also involved with training in the tower that day, was also responsible for the helicopter control position.

    The preliminary report does not assign blame or determine the cause of the close calls, details which will be included in a final report, which often takes a year to complete.

    The new report comes during increased criticism of the US Army’s aviation division — and involved a Black Hawk helicopter from the same unit whose aircraft collided with an American Airlines regional jet on January 29 at Reagan National Airport, killing 67.

    “Is there any unit that when you hear it makes you feel uncomfortable?” asked NTSB investigator Brian Soper at a three-day hearing last month.

    “Sadly, yes,” the witness, medical helicopter executive Rick Dressler, responded. “I’m a former Army aviator, and I’m a retired Air Force officer … and I don’t like saying that 12th Aviation Battalion gives us all pause in the community. And I’m speaking from my group there; we are all very uncomfortable when those two units are operating.”

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    WTOP Staff

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  • Video shows two planes collide while taxiing at airport

    Video shows two planes collide while taxiing at airport

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    Two Delta Air Lines planes collided while both planes were taxiing for takeoff at Atlanta’s Hartsfield-Jackson International Airport. A Delta spokesperson says no one was injured during the collision. The FAA is investigating, and Delta says it’s cooperating with the National Transportation Safety Board.

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  • Five years after 34 died in Conception boat fire, NTSB says Coast Guard hasn’t reformed

    Five years after 34 died in Conception boat fire, NTSB says Coast Guard hasn’t reformed

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    Five years after California’s worst modern maritime disaster, relatives of the Conception boat fire victims are angry about what they call the slow pace of accountability, while a top U.S. safety official says the Coast Guard continues to stall on reforms.

    Thirty-four people died aboard the Conception on Labor Day in 2019, when a fire erupted on the main deck while dozens of divers slept in a windowless bunk room below. In the smoke and chaos, they desperately tried to find a route to safety on the 75-foot dive boat but could not escape.

    Jennifer Homendy, chair of the National Transportation Safety Board, castigated the Coast Guard at a news conference Monday for failing to require safety management systems for small vessels.

    “How many deaths have to occur? How many injuries have to occur? How many families have to stand up here at a press conference grieving for their loves ones before action is taken?” Homendy said as she stood near a plaque at Santa Barbara Harbor that commemorates the Conception victims. “And how many times does Congress, which did it again in 2021, [have to] tell the Coast Guard to take action?”

    Jennifer Homendy, chair of the National Transportation Safety Board, speaks Monday at Santa Barbara Harbor while among family members of those whose died on the dive boat Conception five years ago.

    (Richard Winton / Los Angeles Times)

    Homendy, joined by victims’ relatives, said her agency has made recommendations dating back more than two decades for safety management systems — most recently after the Conception fire.

    She sent a letter Monday to the Homeland Security secretary and head of the Coast Guard asking to implement change “with all possible haste.”

    Coast Guard Vice Adm. Peter Gautier, in a July letter to the NTSB, wrote that it had been “dilgently working” on a notice of a proposed rule making with “all due haste” on safety management systems. But Homendy said that explanation is unacceptable “given the lengthy inaction.”

    Homendy said a safety management system sets out common sense rules and procedures about what training must take place, what emergency drills must be done and how roving watches should be in place to detect fires. These were all massive failures five years ago, she said, when five crew members asleep in the wheelhouse on the top deck were jolted awake by shouts of “Fire! Fire!” shortly after 3 a.m.

    “We’re gonna die,” one passenger was heard during a haunting, 24-second video recorded by passenger Patricia Ann Beitzinger, according to evidence presented at the the 2023 federal criminal trial of Conception Capt. Jerry Boylan.

    The video shows the dark outlines of people trapped in the bunk room as the fire approaches. The voices are muffled and difficult to hear, but prosecutors supplied a transcript to jurors during Boylan’s trial: “There’s got to be a way out.” “There’s got to be more extinguishers.”

    All 33 passengers and one crew member would die of smoke inhalation.

    Inside the bunk room, victims were found with mismatched shoes, one clutched a phone and another, a flashlight. Two were interlocked so tightly they had to be pried apart. As the passengers fruitlessly tried to escape, Boylan and four crew members jumped from the top deck into the waters of Platts Harbor on Santa Cruz Island. Boylan, who had not ordered a roving night watch as people slept, was convicted in 2023 of seaman’s manslaughter and sentenced in May to four years in federal prison.

    The Conception as it appeared at sunrise on Labor Day in 2019, after the fire that left 34 people on board dead.

    The Conception as it appeared at sunrise on Labor Day in 2019, after the fire that left 34 people on board dead.

    (National Transportation Safety Board)

    Investigators with the Bureau of Alcohol, Tobacco, Firearms and Explosives determined that the fire started in a plastic trash can on the main deck on what was to be the final day of a three-day dive trip.

    At the time, such bins were forbidden in all vessels’ sleeping areas, and banned from all compartments on newer boats, but were allowed on old ones such as the Conception, records show.

    But Homendy said Monday that although the fire may have been caused by cigarattes thrown in a trash can, “more than likely” it was lithium ion batteries from phones and photography that were being charged.

    The families have complained for years about what they call foot-dragging by authorities. They also have expressed anger over Boylan remaining free while he appeals his conviction. “We have no rights, we are given no consideration,” said Kathleen McIlvain, who son Charlie McIlvain is among those who died on the Conception.

    “It wasn’t an accident, it was a disaster waiting to happen,” said Vicki Moore, whose husband, Raymond “Scott” Chan, 59, and daughter Kendra Chan, 26, died. Speaking at the harbor Monday, she said that although reforms have been made, without the implementation of safety management systems the tragedy will repeat itself.

    Meanwhile, lawsuits against the Conception’s owners, Truth Aquatics and its boss, Glen Fritzler, remain unresolved.

    NTSB recommendations in the wake of the Conception tragedy for fire detection systems, proper dual escape routes, emergency escape drills and checks on night watches have been implemented. Congress mandated those provisions in December 2020 as part of the Elijah E. Cummings Coast Guard Authorization Act.

    But Homendy said that safety gaps persist even with those reforms, and that the Coast Guard has yet to show how it is monitoring those changes.

    Jerry Boylan, right, captain of the Conception, arrives in federal court during his 2023 trial.

    Jerry Boylan, right, captain of the Conception, arrives in federal court during his 2023 trial.

    (Damian Dovarganes / Associated Press)

    The rear admiral of the Coast Guard said in a 2021 congressional hearing that in weighing new rules, it is required to consider the economic costs and benefits of implementation.

    Homendy said she keeps hearing about the cost, but motioning to the grieving families, she added, “This is the cost.”

    “I am begging the Coast Guard to take action,” she said. “If the companies aren’t going to do it, who’s there to protect safety?”

    Stairway to the upper deck of the Conception.

    A photo from a previous Conception voyage showing the location of restrooms and the stairway to the upper deck, as well as a polyethylene trash can under the stairs. At right, an image is from a 2019 video taken of the stairway, with shelving installed and a trash can below.

    (National Transportation Safety Board)

    An NTSB investigation found that the Conception did not operate a roving watch, a failure that allowed the fire in the middle deck of to go undetected for up to half an hour. It did not determine a cause but blamed Truth Aquatics and Fritzler for a lax safety culture.

    Prosecutors accused Boylan of a slipshod approach to training, leaving everyone on board responsible for their own safety. Boylan’s lawyer said the lack of a roving watch and the approach to safety training had been part of “the Fritzler way” for decades, referring to the boat’s owner.

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    Richard Winton

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  • Rail worker’s death in Ohio railyard highlights union questions about remote control trains

    Rail worker’s death in Ohio railyard highlights union questions about remote control trains

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    The CSX worker who discovered his friend run over by a pair of remote-control locomotives in a railyard last year sees a simple solution to preventing similar deaths in the future: two-person crews.

    But that idea won’t be popular with the railroads that have come to rely heavily on having one person control trains moving around a railyard with a remote control as they take apart and reassemble trains. The tactic that was first approved in 2005 started with two people on the job to watch for hazards, but today one-person remote-control operations are common.

    Using remote control operators helps limit costs by using less experienced workers to move locomotives that help assemble trains — a task that once required licensed engineers who are among the highest-paid rail workers. The Brotherhood of Locomotive Trainmen and Engineers and other unions have been raising concerns about the practice recently, particularly because remote-control trains are now being used in places outside of railyards to make local trips to pick up and drop off cars.

    Railroads are confident the practice is safe based on their experience using it for years. But Federal Railroad Administration spokesman Warren Flatau said the agency is scrutinizing the use of remote control after this death and several other recent incidents. The expanded use of remote-control trains outside of rail yards is also attracting attention.

    The National Transportation Safety Board provided an update on its investigation into the death of Fred Anderson on Wednesday when it posted transcripts of its interviews with the workers involved and other information. Anderson was killed on September 17, 2023, when he stepped in front of two locomotives in CSX’s railyard in Walbridge, Ohio.

    Railroad safety has been in the spotlight ever since last year’s disastrous Norfolk Southern derailment in East Palestine, Ohio, forced evacuations and left residents with lingering health fears after a cocktail of toxic chemicals spilled and burned.

    At the time Anderson was killed, the remote control operator was riding on a ladder on the back of the second locomotive with no view of the front of the train. That practice is perfectly acceptable under federal and railroad rules because earlier in the shift the remote-control operator had cleared the area around the tracks where he was working.

    Anderson and the other carman he was working with, George Oliger, had radioed ahead to get permission to enter the area, but Anderson was still struck by the train. Oliger told investigators afterward that he thinks Anderson’s death would have been prevented if the remote-control operator was on the front of the locomotives or if a conductor or engineer were controlling them from the cab. He said a traditional crew would have likely seen Anderson and rang the bell to alert him to the danger.

    “What does it cost for an engineer for the night? $350? If we had two guys on every crew, to spend $350 to save someone’s life or to make our yard a little bit safer, I think that’s what we need to do, you know. Like I said if there had been a two man crew on that crew that night, we wouldn’t be talking,” Oliger said, according to a transcript of his interview.

    It’s not clear if anyone would have been able to stop the locomotives in time before they hit Anderson, but if someone operating the train had seen him step onto the tracks, they may have been able to warn him. The locomotives were moving at 10 mph (16 kph) when they struck Anderson, and the remote control operator told investigators that he believes it would have taken the length of an engine to stop them at that speed.

    But Randy Fannon, who leads the engineers’ union’s Safety Task Force, said he thinks, “This tragic incident in Ohio involving a remotely operated train, blindly controlled from behind, would not have happened if there had been a locomotive engineer in the cab.”

    Fannon said railyard workers are more alert to the risks presented by remote-control trains, but the union is “adamantly opposed to remotely operated trains being used outside fenced-in yard environments where pedestrians or vehicles could come in contact at rail crossings.”

    CSX and all the unions directly involved aren’t allowed to discuss Anderson’s death until the NTSB completes its investigation, which the agency has said is focused on CSX’s carmen safety procedure training and awareness.

    The Federal Railroad Administration and CSX both put out advisories after Anderson’s death reminding all rail workers that they need to be careful when crossing tracks and should always be aware that a train can move down a track at any time. CSX had its managers stress to all its maintenance workers that they must look both directions before they ever cross tracks.

    The railroad said last year that it wasn’t planning any changes to its remote control operations after Anderson’s death because it appeared that all federal and CSX rules were being followed at the time.

    Safety statistics on railroad crashes are unclear on how safe this practice is because Federal Railroad Administration reports don’t break out those involving remote control trains from incidents involving trains operated by engineers and conductors.

    The Brotherhood of Railway Carmen union has said that three of its members have died in incidents involving remote-control trains since 2015.

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  • Federal officials investigating natural gas explosion in Maryland that killed 2 – WTOP News

    Federal officials investigating natural gas explosion in Maryland that killed 2 – WTOP News

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    The National Transportation Safety Board, which has jurisdiction over pipelines, is investigating a natural gas explosion at a home in Bel Air, Maryland, that killed two people, the agency said Monday.

    At least one person died and two were injured after a Maryland house exploded Sunday amid reports of a possible gas leak, fire officials said.(Courtesy Harford County Fire and EMS)

    ANNAPOLIS, Md. (AP) — The National Transportation Safety Board, which has jurisdiction over pipelines, is investigating a natural gas explosion at a home in Bel Air, Maryland, that killed two people, the agency said Monday.

    Meanwhile, state officials have identified the two people who died, and the state fire marshal’s office said they are focusing on accidental causes because there is no evidence of criminal activity.

    Ray Corkran Jr., the 73-year-old homeowner, died in the Sunday morning explosion, officials said. Jose Rodriguez-Alvarado, a 35-year-old contracted utility employee with Baltimore Gas and Electric, also died, the state fire marshal’s office said.

    Jennifer Gabris, an NTSB spokesperson, confirmed that NTSB pipeline investigators were on the scene Monday in Bel Air, a town about about 30 miles (48 kilometers) northeast of Baltimore.

    Deputy state fire marshals and agents with the federal Bureau of Alcohol, Tobacco, Firearms and Explosives have concluded their on-scene investigation and turned the scene over to insurance representatives, the fire marshal’s office said.

    “Crews have already begun cleaning up the copious debris strewn throughout the neighborhood, and restoration companies are beginning to make repairs to nearby homes,” the fire marshal’s office said in a news release Monday.

    Investigators will now focus on reviewing the evidence and data they collected on Sunday, the fire marshal’s office said. That includes gas and electrical piping, interviews, video surveillance and data from BGE.

    “While the explosion remains under investigation, there is no evidence of criminal activity, and they will continue to focus on accidental causes,” the fire marshal’s office said.

    Firefighters were called to the area around 6:40 a.m. Sunday for a report of a gas leak and an outdoor odor of gas. As firefighters were approaching, they began receiving calls that the house had exploded.

    Two utility workers were in the area to work on a reported electrical issue at the time.

    A woman in a house next door was treated for injuries on the scene.

    Neighbors in the vicinity reported a variety of damage to their homes from the explosion. Twelve families were displaced.

    “Our hearts are broken for the two victims and their families. Our team of highly qualified investigators and our partners at ATF are dedicated to providing an answer that will lead to safer communities,” said Acting State Fire Marshal Jason M. Mowbray. “A tragedy of this size is heart-wrenching for Maryland.”

    More than 60 first responders came to the scene from multiple agencies.

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    © 2024 The Associated Press. All rights reserved. This material may not be published, broadcast, written or redistributed.

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    WTOP Staff

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  • NTSB updates Colonie plane crash

    NTSB updates Colonie plane crash

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    COLONIE, N.Y. (NEWS10) — We have new information about the plane that crashed Monday morning near the William K. Sanford town library in Colonie. NEWS10 reporter James De La Fuente attended a press conference on Tuesday June 18 when the National Transportation Safety Board (NTSB) and local officials gave a brief update into the crash.

    “Before we begin, I would like to express my most sincere condolences to the family and friends of our deceased pilot,” started Lynn Spencer, Air Safety Investigator with the NTSB.

    Spencer says they are not identifying the sole occupant and victim at this time other than to say that she is a Canadian woman.  Spencer says the twin engine personal aircraft was headed to Canada and had made it about a mile and a half from the airport before she says the plane seemed to struggle to gain altitude. “We will be looking at pilot qualifications, the training, the airframe itself and environmental factors,” stated Spencer.

    Spencer also said that because the plane was destroyed by a post-crash explosion her team will be relying on the community for some help in identifying what may have gone tragically wrong. “Of note was that the airplane seemed to have difficulty gaining altitude and then went nearly straight up to about 800 feet and did a loop and then turned left, did at least one roll, and then another left hand turn to the final impact.” She went on to explain how control could have been lost. “When a pilot is struggling to maintain control of the airplane, you often see what looks like acrobatic flying. And it’s simply the pilot’s attempt to deal with everything from an engine failure to a control failure to an environmental event. Anything that upsets the normal flight trajectory.”

    Spencer says she has received a number of reports from the community and eyewitness accounts. “This kind of flight path is typical of an extreme loss of control situation in the cockpit and a pilot attempting to regain control of the airplane. The aircraft struggle was noted by the air traffic controller who canceled the takeoff clearance for the following aircraft because he could see that the departing aircraft was having difficulty.”

    She says the rest of the plane will be packed up and shipped for further investigation. “And later tonight [Tuesday] [the airplane] will be going to Massachusetts to a secure facility there where we will start a full layout, and examination of the airframe and the engines.” Preliminary reports will be completed in the next few weeks and a final report in 18-24 months.

    Maxwell Road between Albany Shaker Road and Old Niskayuna Road have now been reopened to the public.

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    James De La Fuente

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  • Helicopter with six people onboard crashes in San Bernardino County near Nevada border

    Helicopter with six people onboard crashes in San Bernardino County near Nevada border

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    A helicopter carrying six people crashed in San Bernardino County on Friday night near the Nevada border, authorities said.

    A Eurocopter EC 130 helicopter crashed east of the 15 Freeway near Nipton, Calif., about 10 p.m., according to the Federal Aviation Administration. Six people were onboard.

    It is unknown if any of the passengers survived.

    No other details were available about where the helicopter’s flight originated from or about its destination.

    The FAA and the National Transportation Safety Board are investigating the crash.

    This story is developing and will be updated as more information becomes available.

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    Carlos Lozano

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  • Small plane that crashed off California coast was among a growing number of home-built aircraft

    Small plane that crashed off California coast was among a growing number of home-built aircraft

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    LOS ANGELES (AP) — A small airplane that crashed into the ocean off the California coast on Sunday was constructed piece by piece over nearly a decade, one of tens of thousands of home-built aircraft that are part of a high-flying hobby taking off across the country.

    Federal investigators said they believe four people were aboard the single-engine Cozy Mark IV when it went down in the evening just south of San Francisco. No survivors were found and only one body had been recovered from the waters near Half Moon Bay and identified as of Thursday.

    The names of the pilot and two other passengers were not released. The plane was registered to an Oakland-based company called Winged Wallabies, Inc., according to Federal Aviation Administration records.

    There have been no official indications of what went wrong, but a witness reported hearing an engine losing power and cutting out.

    Thane Ostroth, a retired dentist who began building the aircraft in 1999 and flying it in 2008, said he sold the plane last year to a young, experienced and enthusiastic pilot from Australia for around $100,000, which is about what he estimated went into the project over the decades.

    Ostroth said the buyer, in his late 20s, knew a lot about planes. He landed the plane perfectly on his first test flight, which is not easy to do.

    “I told him, ‘That was well done,’” Ostroth recalled. “He said, ‘Thank you. I’ll buy the plane.’”

    Authorities have not said whether the plane’s owner was among those on board.

    Ostroth said he heard about the crash in an online chat group for pilots and builders of Cozy aircraft, a class of planes constructed by individuals rather than mass-produced by companies.

    He said it was “traumatic” to know the plane he had spent so much time on had crashed with people on board.

    “It’s just a horrible feeling,” Ostroth said.

    Like commercial aircraft, all home-built planes are required by the FAA to be inspected annually for air worthiness. Cozy aircraft have the same safety record as commercially built planes of similar size, said aeronautical engineer Marc Zeitlin, who consults with the National Transportation Safety Board on crash investigations involving Cozy aircraft, including this one.

    More than 33,000 amateur-built aircraft are licensed by the FAA, a figure that has tripled since the 1980s.

    The administration designates any non-commercial, recreational aircraft as “experimental.” Those can include planes built from kits with some prefabricated parts or from plans in which the builder buys or manufactures and assembles all the parts.

    The four-seat Mark IV, at just over 16 feet (5.1 meters) long with a 28-foot (8.5-meter) wingspan, is a popular plane among the growing number of aviation hobbyists who build their own aircraft. Zeitlin owns one himself that he takes on day trips and cross-country voyages.

    “The misconception is that these are put together by baling wire and glue,” said Zeitlin, CEO of California-based Burnside Aerospace. “But they are built using aircraft methodology.”

    The Mark IV has a “canard” design, with a small forewing placed to the front of the main wing, making it reminiscent of a duck stretched out in flight. It is lightweight, only about 1,050 pounds (475 kilograms) empty, with the parts fitted together with epoxy.

    With a top speed approaching 200 mph (322 kph), it is fast, stable and fuel-efficient, Zeitlen said.

    “Like a sports car in the sky,” he said. “Very fun to fly.”

    Ostroth said he bought the plans for his Cozy for about $500 and started putting it together in a friend’s basement in Michigan. Eventually they moved construction to the home’s garage and then built a barn in the backyard for the final steps.

    “The plans come with a list of authorized suppliers of parts,” said Ostroth, who now lives in Florida. “You buy foam, you buy fiberglass, you buy metal parts from all the manufacturers. And you slowly piece it together.”

    Help can be found from other enthusiasts who post tips and advice in online forums.

    Ostroth flew the aircraft regularly for 15 years. He called it “a wonderful little plane.”

    Sunday’s crash was reported around 7 p.m. by a 911 caller who said the plane was in obvious distress and appeared to go down toward the water near Ross’ Cove, according to the San Mateo County Sheriff’s Office.

    The U.S. Coast Guard said a helicopter and boat crew looked in a 28-square mile (73-square-kilometer) area for nearly six hours before calling off the search around mid-morning Monday. A few hours later, a woman’s body was found by a commercial fishing boat crew. The San Mateo County Coroner’s Office identified her as Emma Willmer-Shiles, 27, of San Francisco.

    The National Transportation Safety Board said its investigators arrived on scene Tuesday to document the wreckage and interview witnesses. A preliminary report is expected within 30 days.

    ___

    Associated Press writer John Antczak in Los Angeles contributed to this report.

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  • Door plug that blew off Alaska Airlines plane in-flight found in backyard

    Door plug that blew off Alaska Airlines plane in-flight found in backyard

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    The National Transportation Safety Board says the plug covering an unused exit door that blew out minutes into an Alaska Airlines flight Friday night has been found. The agency’s head said the discovery could prove vital in the investigation of the cause of the blowout, which forced the Boeing 737 Max 9 to return to Portland, Oregon minutes after takeoff.

    The Federal Aviation Administration grounded all of the types of Boeing 737 Max 9s involved until it’s “satisfied that they are safe,” an FAA spokesperson said in a statement Sunday.  

    In a news conference Sunday night, National Transportation Safety Board Chair Jennifer Homendy said the plug was found near Portland in the backyard of a schoolteacher she identified only as Bob. “We are really pleased that Bob found this,” she said.

    The Reuters news agency says she had earlier told reporters the aircraft part was a “key missing component” to determine why the accident occurred.

    Homendy told reporters pilots reported that the same plane experienced three pressurization warnings, from cockpit dashboard lights, between Dec. 7 and Jan. 4. At least one occurred in-flight.

    The plane was just weeks old, delivered at the end of October. Alaska Airlines maintenance crews checked and cleared the light after each illumination.

    On the day before the blowout, Homendy said, the carrier ordered that the plane involved couldn’t make any long flights over water so it could “return very quickly to an airport” if the warning light appeared again. She stressed that the light might not be related to Friday’s incident. In addition, more maintenance work was ordered — basically a deeper dive into why the light kept illuminating — but none was done before Friday night’s flight.

    Homendy described a chaotic scene in the plane’s cockpit and directly outside the cockpit after the blowout. 

    She said the flight crew heard a bang and the cockpit “door flew open” from depressurization, so they immediately put their masks on, but communication in the cockpit and between the crew members in the cabin and cockpit were very difficult.

    The force of the depressurization slammed the cockpit door into the front restroom door, damaging the restroom door, and it took a flight attendant three tries to get the cockpit door to close again, Homendy said.

    She noted that the first officer lost her headset and the captain had a portion of her headset pulled off. The captain and first officer couldn’t hear anything in their damaged headsets once they were recovered so they used the overhead speaker to hear.

    A quick reference checklist kept within easy reach of the flight crew also flew out the door, Homendy said, adding that it was incredibly loud and chaotic on board.

    Homendy said the flight data recorder and cockpit voice recorder were sent to NTSB labs on Sunday to be read. But CBS News senior transportation and national correspondent Kris Van Cleave reports the voice recorder won’t help investigators:

    The Reuters news agency says the NTSB has been pressing to have the cockpit voice-recording requirement increased to 25 hours. According to Reuters, Homendy said the FAA proposed a rule in November that would increase the requirement, but only for newly manufactured aircraft.

    The FAA’s Emergency Airworthiness Directive grounding many of the the Max 9s impacts about 171 worldwide. Such directives are issued “when an unsafe condition exists that requires immediate action by an owner/operator,” according to the agency.

    “The FAA’s first priority is keeping the flying public safe,” the FAA spokesperson said. 

    What happened on the Alaska Airlines flight?

    The flight from Portland, Oregon to Ontario, California was minutes into its journey and had reached approximately 16,000 feet when the door plug blew off, an NTSB official said during a Saturday press briefing. The gaping hole in the side of the jet opened up where Boeing fits a plug to cover an emergency exit that the airline doesn’t use, The Associated Press explained.

    Homendy called the event an “accident, not an incident.” She said the plane was forced to return to Portland International Airport just minutes after takeoff “after a mid-cabin door plug … departed the airplane, resulting in rapid decompression.”

    The two seats next to the part that tore off were unoccupied, Homendy said. None of the 171 passengers or six crew members suffered serious injuries, Homendy said. The NTSB said Sunday that the plane didn’t sustain any structural damage.

    Who is investigating the incident?

    The FAA, NTSB, Boeing, Alaska Airlines, Airline Pilots Association and Association of Flight Attendants are all investigating, officials said. 

    The FBI is also helping local law enforcement locate parts that came off during flight. A spokesperson for the FBI’s Portland office said the agency remained “in an on-call status.”

    The NTSB has asked anyone with pictures and videos to reach out to witness@ntsb.gov.

    How are airlines and Boeing responding?

    In the U.S., only Alaska Airlines and United Airlines use the Boeing 737 Max 9 aircraft.

    Alaska Airlines temporarily grounded its entire 737-9 MAX fleet, pending inspections, the company said. The airline said it canceled 160 flights Saturday, impacting roughly 23,000 passengers, another 170 flights on Sunday, impacting about 25,000 passengers, and 60 for Monday. “We expect additional significant cancellations through the first half of the week,” the airline said Sunday night.

    United said Sunday that, “Service on United’s Boeing 737 MAX 9 aircraft remains temporarily suspended while it conducts inspections required by the FAA. We’re continuing to work with the FAA to clarify the inspection process and requirements for returning all MAX 9 aircraft to service. We are working with customers to re-accommodate them on other flights and in some cases have been able to avoid cancellations by switching to other aircraft types.”

    Agence France-Presse reports that carriers and regulators worldwide grounded some versions of the Boeing 737 MAX 9 jetliners, Turkish Airlines among them.

    Boeing has so far delivered about 218 of the 737 MAX planes worldwide, the company told AFP.

    A Boeing spokesperson said it fully supported “the FAA’s decision to require immediate inspections of 737-9 airplanes with the same configuration as the affected airplane.”

    Boeing President and CEO Dave Calhoun on Sunday told employees he will be holding a “company-wide webcast focused on safety” on Tuesday. He also canceled a leadership summit for Boeing vice presidents that was supposed to take place Monday and Tuesday to “focus on our support to Alaska Airlines and the ongoing National Transportation Safety Board investigation, and any of our airline customers experiencing impact to their fleets,” Calhoun wrote.

    Past investigations into Boeing 737 planes

    There are currently two versions of the Boeing 737 in service: the Max 8 and the Max 9.

    In 2018, a Lion Air flight on a Boeing 737 Max 8 plane crashed into the ocean. The following year, an Ethiopian Airlines plane of the same model crashed shortly after takeoff. More than 300 people died in the two crashes. The jets were grounded in March 2019. The Boeing 737 Max was allowed to return to service late in 2020.

    In April, Boeing paused 737 Max production over an issue with aircraft parts.

    Homendy said after Friday’s incident that the NTSB does not suspect there is an overall design problem with the plane. 

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  • Alaska Air blowout’s missing 737 Max fuselage chunk so hard to find investigators are asking for public’s help

    Alaska Air blowout’s missing 737 Max fuselage chunk so hard to find investigators are asking for public’s help

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    The National Transportation Safety Board appealed to the public to help locate the missing door that suffered a blowout on Alaska Airlines Flight 1282 as the agency began the process of finding out what went wrong.

    “We’ve now determined based on our definition of substantial damage that this is an accident, not an incident,” NTSB chair Jennifer Homendy said at a Saturday night press briefing in Portland, Oregon. “We are very fortunate this didn’t end up in something more tragic.”

    The plane was carrying 171 passengers and six crew from Portland to Ontario, California on Jan. 5 when the crew reported a pressurization issue. What followed was a rear left part of the fuselage blowing out, leaving the hole resembling the opening for a door. The aircraft returned to Portland about 20 minutes after takeoff, having reached an altitude of about 16,000 feet (4,800 meters).

    Read More: After Boeing 737 Max planes crashed and killed hundreds of people about five years ago, one just lost a chunk of its fuselage in midair

    On the Max 9, Boeing includes a cabin exit door located just behind the wings, but before the rear exit door. This is activated in dense seating layouts to meet evacuation requirements. The doors are not activated on Alaska Air aircraft and are permanently “plugged.”

    No one was seated in the immediate two seats — 26 A and B — nearest the plugged door, Homendy said. The Federal Bureau of Investigation is also helping local law enforcement track down the door.

    Flight data and cockpit voice recorders from the plane will be sent to a laboratory Sunday for analysis, the NTSB said.

    Homendy said the NTSB investigation will include a look at the Federal Aviation Administration’s oversight of Boeing Co. and the manufacturer’s process for planemaking on the affected aircraft type. She stressed everything would be studied at the early stages, and nothing would be excluded until it could hone in on the causes of interest.

    Subscribe to the Eye on AI newsletter to stay abreast of how AI is shaping the future of business. Sign up for free.

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    Danny Lee, Bloomberg

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  • Two pilots were killed in a collision at a Reno air show | CNN

    Two pilots were killed in a collision at a Reno air show | CNN

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    CNN
     — 

    Two pilots were killed when their planes collided Sunday during the National Championship Air Races and Air Show in Reno, Nevada, organizers of the event said.

    “Around 2:15 p.m. this afternoon, at the conclusion of the T-6 Gold race, upon landing, two planes collided and it has been confirmed that both pilots are deceased,” the Reno Air Racing Association said in a statement posted on Facebook.

    In a later statement, organizers identified the two pilots as Nick Macy and Chris Rushing.

    “Both expertly skilled pilots and Gold winners in the T-6 Class, Macy piloted Six-Cat and Rushing flew Baron’s Revenge,” the updated statement said. “Families of both pilots have been notified and support services are onsite as they deal with this tragedy.”

    No other injuries were reported, it added.

    The remainder of the races were canceled, organizers said.

    The National Transportation Safety Board said in a statement sent to CNN it is investigating the cause of the crash. The agency, which is leading the probe, identified the two aircraft as a North American T-6G and North American AT-6B, and said they had just completed the race.

    “The wreckage of each plane came to rest one-half mile from each other,” NTSB said, adding the wreckage will be taken to an off-site facility for analysis.

    Event organizers said they are cooperating with the NTSB, the Federal Aviation Administration and “all local authorities to identify the cause of the accident and ensure that all of our pilots, spectators and volunteers have the necessary support during this time.”

    The event, which has been running for more than five decades, prides itself in being an “institution for northern Nevada and aviation enthusiasts from around the world,” according to its website. Over the past decade, the event has brought more than a million spectators and “generated more than $750 million” for the regional economy, according to the site.

    This is not the event’s first fatal crash. A pilot was killed last year in a plane crash during a race and In 2011, 11 people were killed and more than 60 others injured when a plane veered out of control and slammed into spectators.

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  • Safety investigators will look into how an engine caught fire on a Boeing 737 Max

    Safety investigators will look into how an engine caught fire on a Boeing 737 Max

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    WASHINGTON (AP) — Federal safety officials say they will investigate an engine fire that was discovered on a United Airlines Boeing 737 Max after the plane landed in Newark, New Jersey.

    The National Transportation Safety Board disclosed the investigation Friday, when it issued a preliminary report on the June 28 incident. No one was injured.

    Boeing declined to comment, referring inquiries to the NTSB and United, which said it too was investigating.

    Firefighters in Southern California are battling three separate brush fires that started Friday afternoon amid the hottest weather of the year so far.

    An early morning fire has killed multiple animals at a wildlife center in Florida. Officials say a fire broke out around 3 a.m.

    Fifty years ago, millions of files were destroyed in a huge fire at the Military Personnel Records Center in suburban St. Louis.

    Crews extinguished the intensely burning fire aboard a cargo ship docked in New Jersey after nearly a week and are now beginning their investigation into the blaze that resulted in the deaths of two firefighters.

    One of the plane’s two engines caught fire after the plane completed a flight from Fort Lauderdale, Florida.

    Pilots said they noticed a fire-warning indicator for the left engine as they taxied to the gate at Newark Liberty International Airport. They shut down the engine and discharged a bottle of fire retardant, and the warning indicator flicked off, according to the NTSB.

    There was no smoke or fire coming from the engine, but the plane was towed to the gate, where maintenance crews saw signs of fuel leaking from the engine, and heat damage inside the engine cover, the NTSB said.

    The NTSB kept the engine for its investigation. Federal Aviation Administration records indicate the plane was built in late 2020.

    The flight carried 179 passengers and five crew members.

    The NTSB said the investigation will include representatives from Boeing, engine maker CFM International, United Airlines and the FAA.

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  • 6 killed in small plane crash in Southern California

    6 killed in small plane crash in Southern California

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    6 killed in Southern California plane crash


    6 killed in Southern California plane crash

    00:17

    All six people aboard a twin-engine plane were killed when it crashed amid poor visibility while trying to land at a Southern California airport early Saturday morning, officials said, sparking a small brush fire in the process. 

    The 1979 Cessna Citation 550 business jet crashed at around 4:15 a.m. local time near the French Valley Airport in Murrieta, National Transportation Safety Board investigator Elliot Simpson said in a Saturday night news conference. Murrieta is located in Riverside County. 

    The plane had taken off at about 3:15 a.m. from Harry Reid International Airport in Las Vegas, according to the NTSB and Federal Aviation Administration. 

    6 killed in small plane crash in Southern California
    A Cessna carrying six people crashed in a field near French Valley Airport in Murrieta, California, on July 8, 2023. All six people aboard were killed.  

    Irfan Khan/Los Angeles Times via Getty Images


    The Riverside County Fire Department tweeted that the plane came “down in a field” and became “fully involved in fire.” The blaze burned “approximately one acre of vegetation” before being contained at about 5:35 a.m.

    The plane crashed about 500 feet short of the runway amid poor visibility due to weather conditions, Simpson disclosed.  

    “Shorty before landing, the marine layer began to envelope the area with low ceilings and visibilities,” Simpson said. “The pilot reported to air traffic control that he was gonna perform a missed approach, which generally happens when the pilot can’t see the runway environment.”

    He noted that the plane had landed at French Valley Airport multiple times before. 

    All six people aboard were pronounced dead at the scene, the Riverside County Sheriff’s Office said in a news release. Simpson said all the victims were adults. No names were immediately released. 

    The FAA and National Transportation Safety Board are investigating. The NTSB will release a preliminary report on the crash within about two weeks.

    This is the second crash in the area in less than a week. CBS Los Angeles reported that another Cessna crashed near the French Valley airport shortly before 2 p.m. Tuesday, killing one person and injuring three others. 

    The deceased victim was identified as 39-year-old Temecula resident Jared Newman, the father of the three surviving passengers, according to CBSLA. He was reportedly operating the aircraft under a training license, which is prohibited by federal regulations. 

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  • Rail union says Virginia derailment renews questions about Norfolk Southern’s safety practices

    Rail union says Virginia derailment renews questions about Norfolk Southern’s safety practices

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    The union that represents locomotive engineers says a Thursday night coal train derailment in Virginia is renewing questions about Norfolk Southern’s safety practices.

    The derailment happened coming down out of the Appalachian Mountains near Elliston about 20 miles (32.19 kilometers) outside Roanoke. Fortunately, it involved coal cars and not hazardous materials like those that generated a huge plume of black smoke and forced evacuations in the eastern Ohio town of East Palestine after a different Norfolk Southern train derailed in February. That Ohio derailment triggered concerns nationwide about railroad safety and prompted calls for reforms from members of Congress and regulators.

    “We’re just lucky right now that it’s coal. If it had been ethanol or LP gas or chlorine or anything like that, it could have been a totally different situation,” said Randy Fannon, who leads the Brotherhood of Locomotive Engineers and Trainmen union’s safety task force.

    The Scottish government has proposed decriminalizing possession of all drugs for personal use to tackle one of Europe’s highest overdose death rates.

    Zimbabwe’s main opposition party has gone to court to challenge a police decision to ban a rally it wants to hold in the buildup to what will be highly scrutinized elections next month.

    The rain returned to Wimbledon on Day 6 of the grass-court tournament. Only one match was completed before play was suspended on all outside courts.

    Hundreds of people have marched in South Korea’s capital demanding Japan scrap its plans to release treated wastewater from the damaged Fukushima nuclear power plant.

    Nineteen cars on the Virginia coal train derailed around 7:45 p.m. Thursday but remained upright and none of the coal spilled.

    Before the derailment, the crew received a critical alarm from a trackside detector that a wheel bearing was overheating. But unlike in the East Palestine derailment where the crew received little warning, the crew was able to safely stop the Virginia train after it was alerted to the potential hazard.

    The train’s conductor found the railcar that triggered the alarm and confirmed the bearing was overheating. But a spokesman for the railroad said all the components appeared to be intact during a visual inspection.

    Federal Railroad Administration spokesman Warren Flateau said the railroad decided to try and move the train to a siding, where the crew could safely set out the car with the overheating bearing without blocking the main track. But the train derailed before it reached the siding.

    National Transportation Safety Board officials said late Friday they would investigate the Virginia derailment. While union officials and the railroads involved in an NTSB investigation aren’t allowed to speak publicly before that agency releases its findings, Fannon discussed the details of the crash Friday afternoon when the FRA was still leading the investigation. The NTSB had not taken the lead at that time.

    Fannon said someone at the railroad’s headquarters in Atlanta who was working on the “hot box detector desk” told the crew to go ahead and move the train 8 miles (12.87 kilometers) down the track. The crew told union officials that they weren’t comfortable with moving the train at the track speed of roughly 40 mph, so they kept the speed to around 20 mph. But the train still derailed.

    Spokesman Tom Crosson said Norfolk Southern will use this derailment to help inform changes it is making to improve safety.

    “This derailment should never have happened. It is unacceptable,” Crosson said. “We are working to achieve our goal of being the gold standard for safety in the railroad industry, and this incident strengthens our resolve.”

    Both the FRA and the NTSB said they were investigating Norfolk Southern’s safety practices following the East Palestine derailment and several others in the past couple years.

    The NTSB is doing a detailed investigation to determine everything that contributed to the East Palestine derailment, but investigators said in their preliminary report that an overheating bearing on a rail car carrying plastic pellets likely caused the derailment. The resulting fire burned for days as several cars carrying hazardous materials spilled their contents. Then officials decided to blow open five vinyl chloride cars and burn that chemical because they were worried those tank cars might explode.

    “NS is still in the spotlight and they’re going to remain that way until they make some changes,” Fannon said.

    In years past before Norfolk Southern began overhauling its operations in 2019 and making widespread job cuts, Fannon said the railroad typically would have sent a mechanical inspector to examine the car after an overheating bearing was found to determine if it was safe to move the train. That doesn’t happen anymore after all the cuts to the ranks of inspectors.

    “I think the key to this is no qualified mechanical person inspected it,” Fannon said.

    Norfolk Southern, like all the major freight railroads, has streamlined its operations over the past several years to reduce costs by relying more on running fewer, longer trains so it doesn’t need as many crews or locomotives. The Brotherhood of Locomotive Engineers and Trainmen and the other rail unions have said the changes make railroads riskier, spreading employees thin and making it difficult to take the time to properly inspect cars or complete needed preventative maintenance.

    The railroads have defended their safety record.

    Railroad officials have said they don’t believe the cuts jeopardized safety, and they emphasize that they continue to meet the minimum federal standards. Norfolk Southern’s CEO Alan Shaw has said he believes NS is a safe railroad and that he is committed to improving that.

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  • 7 injured in turbulence on Hawaiian Airlines flight to Australia

    7 injured in turbulence on Hawaiian Airlines flight to Australia

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    HONOLULU (AP) — A Hawaiian Airlines flight from Honolulu to Sydney hit severe turbulence, injuring seven people on board.

    The plane was carrying 163 passengers and 12 crew members on Thursday when it “encountered unexpected severe turbulence approximately five hours into the flight,” said a statement from the airline.

    “The plane just dropped,” passenger Sultan Baskonyali told ABC News. “We weren’t prepared.”

    Sun’s out, guns out? Not on Hawaii’s world-famous beaches. Beginning Saturday, a new law prohibits carrying a firearm on beaches, as well as banks and restaurants that serve alcohol.

    HONOLULU (AP) — A man accused of firing into a large crowd at a Hawaii cockfight in a shooting that killed two people pleaded not guilty to murder and other charges Thursday.

    Police in Hawaii have vowed to step up illegal gambling enforcement after one of the most serious shootings in state history called attention to the dangers that come with cockfighting.

    A Hawaii surfer credits his faith in God for surviving an Easter shark attack. Mike Morita said Wednesday from a hospital bed that he’s at peace with losing his right foot to Sunday’s shark attack at his regular Honolulu surfing spot known as Kewalos on the south shore of the island of Oahu.

    She described one man going upward, hitting his head on the ceiling and dropping back down.

    Airport medics assessed and released three injured passengers when the flight landed in Sydney, the airline said. One passenger and three flight attendants were referred to hospitals for evaluation. The flights attendants have since been released, the airline said Monday, but added that it was waiting to hear from the passenger.

    “I haven’t heard from the airline at all even though both my children who were on the flight sustained minor injuries,” another passenger, Tara Goodall, told The Associated Press Monday.

    They were returning home to Sydney after visiting Hawaii — the first overseas trip for her two sons. It was difficult, she said in text messages, “seeing your kids being thrown around the plane cabin” and being unable to make them feel safe.

    She said she wasn’t yet ready to discuss the turbulence in more detail because she was still upset and emotional about it.

    “Our immediate priority is to continue to care for our passengers and crew affected by this turbulence event, and we thank Sydney airport first responders for their swift assistance,” the airline said.

    Last year, severe turbulence injured 25 people on board a Hawaiian Airlines flight. Four passengers and two crew members were seriously hurt. The plane sustained minor damage.

    The captain of the Dec. 18 flight from Phoenix to Honolulu told investigators that conditions were smooth with clear skies when a cloud shot up in front of the plane, and that there was no time to change course, according to a report by the National Transportation Safety Board.

    Hawaiian Airlines Chief Operating Officer Jon Snook said at the time that such turbulence is unusual, noting that the airline had not experienced anything like it in recent history. The sign to fasten seatbelts was on at the time, though some of the people injured were not wearing them, he said.

    It happened about 40 minutes before landing in Honolulu, according to the NTSB report.

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  • Airport Employee Killed After Being ‘Ingested’ By Plane Engine

    Airport Employee Killed After Being ‘Ingested’ By Plane Engine

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    An employee for the San Antonio International Airport was killed after being “ingested” by a plane engine on Friday night, NBC affiliate WOAI reported.

    The incident occurred as Delta Flight 1111 landed at the airport and taxied to the gate using a single engine, according to the report. Exact details surrounding the employee’s death, including their identity, have not been released, but the investigation is ongoing.

    “We are deeply saddened by this incident and are working with authorities as they begin their investigation,” the San Antonio International Airport said in a statement to WOAI. “We will share more information as details become available.”

    “We are heartbroken and grieving the loss of an aviation family member’s life in San Antonio. Our hearts and full support are with their family, friends and loved ones during this difficult time,” Delta said in a statement to HuffPost on Sunday.

    The National Transportation Safety Board, which is investigating the incident, and the San Antonio airport did not immediately respond to HuffPost’s request for comment.

    In December, an American Airlines ground crew member was killed in a similar accident in Montgomery, Alabama, which led to a $15,625 fine from the Occupational Health and Safety Administration.

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  • US fighter jets responded to an aircraft with an unresponsive pilot near DC. The aircraft ultimately crashed in Virginia | CNN

    US fighter jets responded to an aircraft with an unresponsive pilot near DC. The aircraft ultimately crashed in Virginia | CNN

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    CNN
     — 

    US F-16 fighter jets caused a sonic boom across the Washington, DC, region Sunday as they scrambled to reach an unresponsive aircraft that ultimately crashed in Virginia, officials said.

    A US official said the F-16s did not shoot down the aircraft and that it is typical for the Federal Aviation Administration to call in jets if someone is flying unsafely.

    The pilot of the civilian aircraft was unresponsive as the F-16 fighter jets attempted to make contact, according to a news release from the Continental US North American Aerospace Defense Command Region.

    The F-16 jets were “authorized to travel at supersonic speeds,” which resulted in the sonic boom heard in the Washington, DC, area.

    The F-16s used flares “in an attempt to draw attention from the pilot,” the release added.

    The civilian aircraft, a Cessna 560 Citation V, was intercepted by the NORAD jets around 3:20 p.m. and ultimately crashed near the George Washington National Forest in Virginia.

    “The pilot was unresponsive and the Cessna subsequently crashed near the George Washington National Forest, Virginia,” the release said. “NORAD attempted to establish contact with the pilot until the aircraft crashed.”

    Four people were on board the aircraft, which overshot its planned destination by 315 miles before crashing, sources familiar with the investigation said.

    Search efforts were still underway by state and local authorities Sunday evening, Virginia State Police told CNN.

    State police were notified around 3:50 p.m. of a possible aircraft crash in the Staunton/Blue Ridge Parkway region, the agency said.

    Nothing has been located at this time, it added.

    The National Transportation Safety Board said on Twitter it was investigating the crash.

    The military aircraft caused a sonic boom heard across the Washington, DC, metropolitan region.

    “We are aware of reports from communities throughout the National Capital Region of a loud ‘boom’ this afternoon,” DC Homeland Security & Emergency Management said on Twitter.

    There is no threat at this time, the agency added.

    Earlier, the FAA said in a statement that a Cessna Citation crashed in southwest Virginia Sunday.

    The aircraft took off from Elizabethton Municipal Airport in Elizabethton, Tennessee, and was bound for Long Island MacArthur Airport in New York.

    The aircraft crashed into a mountainous terrain in a “sparsely populated area”, according to FAA.

    The US Capitol Complex was placed on “an elevated alert” when the small aircraft flew near the area on Sunday afternoon, according to a statement from US Capitol Police.

    “This afternoon, our officials were working closely with our federal partners to monitor an unresponsive pilot who was flying an airplane near the National Capital Region. The U.S. Capitol Complex was briefly placed on an elevated alert until the airplane left the area,” the statement said.

    The US Secret Service said they did not alter their posture for keeping President Joe Biden secure after the incident. Biden was golfing at the Andrews Air Force Base golf course near Joint Base Andrews in Maryland.

    The incident “had no impact on Secret Service,” spokesperson Anthony Guglielmi said in a Sunday statement.

    The President has been briefed on the incident, according to a White House official.

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